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Rex speed shop RMK6-12V on 74 Dt 250 upgrade from 6 volt to 12 volt timing issue
- Ericb1318
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Rex speed shop RMK6-12V on 74 Dt 250 upgrade from 6 volt to 12 volt timing issue was created by Ericb1318
Has anyone upgraded their 1974 dt250 to a Rex’s speed shop 12 volt kit? The actual kit is a RMK6-12 volt. I’m having a heck of a time getting this thing timed. I have the timing light on it and it is about perfect no matter how much I rotate the stator. Rex suggested rotating it 1mm at a time which I did. The bike will run and idle fine. At 5500 rpm it starts to cut out. Was running fine before I put the kit on it. It has always been finicky with timing but I can’t seem to find the sweet spot this time. Any help will be much appreciated.
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- RT325
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Replied by RT325 on topic Rex speed shop RMK6-12V on 74 Dt 250 upgrade from 6 volt to 12 volt timing issue
Just my random thoughts & timing isn't an exact science as regards misfiring at 5500rpm. I think you might be looking for the wrong cause but happy to be proven wrong. You say "was running fine before fitting the kit" so is there a wiring fault the way they're connected. I live in the past--& still have points ignition. I won't say exhaust or carb because was ok on original mag--but i'll say it anyway lol.
The following user(s) Liked this Post: Ericb1318
14 Apr 2026 15:40
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- Ericb1318
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Replied by Ericb1318 on topic Rex speed shop RMK6-12V on 74 Dt 250 upgrade from 6 volt to 12 volt timing issue
Thank for the advice RT325. I 100% agree with you about it possibly being the carb or something other than the timing. I’m going to take the kit off this weekend and put the points back on it to test my theory. These are old machines so it is quite possible something else broke during the change out. Almost sounds like the pipe is clogged but I had one of the guys on the site make it a “sleeper” pipe a few years ago. It could be plugged I guess. Changing back to stock will verify.
The following user(s) Liked this Post: RT325
14 Apr 2026 20:30
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